I got a call from the machine shop after 5 weeks.  They wanted me to come in to discuss what they had found.  THey did a leakdown test and found cylinders 3 and 7 were leaking 90%.  They pulled that cylinder head and found 2 sticky exhaust valves and excessivly cut valve seats.  The heads were purchased from Areohead Racing many years ago.  That head needed a couple new valves, all new valve seats and new guides.  The other head was working OK but I didn't trust it.  It would have needed the same work.  I decided to bring in the original heads instead of trying to fix those.
A couple days after dropping off the original heads, I went in to see what they found with those.  Those heads needed all new valves, guides and one valve seat.  Right as I was leaving, the manager said,"Oh, by the way, the intake manifold is cracked."  He took be back to see the intake and sure enough.  There was a big crack starting in the choke thermostat well and extending all the way over to the EGR valve opening.  That was the original intake with the correct casting date.  Luckily I had a spare intake that checked out good.  The new intake is slightly different but it's close.
I picked up the engine last Tuesday.

Cleaned and painted it on Wednesday.

Dropped it back in on Thursday.

I worked on it Friday night and most of the day on Saturday.  After everything was put back together, I installed the new repro green top battery and it fired right off.  I was tired so I havn't timed it yet but it runs and sound decent.  Here's a quick video I took of it running.
http://www.youtube.com/watch?v=tGKhYa6QDfc